Banner Top
Monday, April 29, 2024

A series of failures led to the crash of a Lion Air flight, which killed 189 people and led to the grounding of the Boeing 737 Max, a report has found.

Investigators said faults by Boeing, Lion Air and pilots caused the crash.

Five months after the disaster in October last year, an Ethiopian Airlines plane crashed, killing all 157 people on board, which led to the grounding of the entire 737 Max fleet.

Faults with the plane’s design have been linked to both crashes.

On Friday, air crash investigators in Indonesia released their final report, detailing the list of events that caused the Lion Air jet to plunge into the Java Sea.

“From what we know, there are nine things that contributed to this accident,” Indonesian air accident investigator Nurcahyo Utomo told reporters at a news conference.

“If one of the nine hadn’t occurred, maybe the accident wouldn’t have occurred.”

What does the report say?

The 353-page report found the jet should have been grounded before departing on the fatal flight because of an earlier cockpit issue.

However, because the issue was not recorded properly the plane was allowed to take off without the fault being fixed, it said.

Further, a crucial sensor – which had been bought from a repair shop in Florida – had not been properly tested, the report found.

That sensor fed information to the plane’s Manoeuvring Characteristics Augmentation System – or MCAS. That software, which is designed to help prevent the 737 Max from stalling, has been a focus for investigators trying to find the cause of both the Lion Air and Ethiopian Airlines crashes.

Indonesian investigators identified issues with the system, which repeatedly pushed the plane’s nose down, leaving pilots fighting for control.

It showed there were incorrect assumptions about how the MCAS control system would behave and that the “deficiencies” had been highlighted during training.

Further, the report found that the first officer, who had performed poorly in training, struggled to run through a list of procedures that he should have had memorised.

He was flying the plane just before it entered into the fatal dive, but the report said the captain had not briefed him properly when he handed over the controls as they struggled to keep the plane in the air.

The report also found that 31 pages were missing from the plane’s maintenance log.

Indonesian investigators have previously said mechanical and design problems were key factors in the crash of the Lion Air plane.

How has Boeing responded?

Indonesian authorities laid out some recommendations for Boeing in the report, including that it redesign MCAS and provide adequate information about it in pilot manuals and training.

In a statement, Boeing said it was “addressing” the recommendations from Indonesia’s National Transportation Safety Committee.

The planemaker said it was “taking actions to enhance the safety of the 737 Max to prevent the flight control conditions that occurred in this accident from ever happening again”.

On Tuesday, the firm ousted Kevin McAllister, chief executive of Boeing Commercial Airplanes, making him the most senior official to leave the company since the two crashes.

Boeing also said it expected the 737 Max to resume flying before the end of the year. The company said “we look forward to continuing to work together” with Lion Air in the future.

A Lion Air spokesman said the crash was an “unthinkable tragedy” and it was essential to take immediate corrective actions to ensure a similar accident never occurred again.

What has been the fallout for Boeing?

The pressure on Boeing to explain what it knew about the problems with the 737 Max has been kept up following recent revelations that employees had exchanged messages about issues with MCAS while the plane was being certified in 2016.

In documents provided by Boeing to lawmakers, a pilot wrote that he had run into unexpected trouble during tests. He said he had “basically lied to the regulators [unknowingly]”.

Boeing said this week it had developed a training update and that it expected regulators to allow the planes to return to the skies before the beginning of 2020.

The grounding of the 737 Max has taken a toll on the planemaker.

Profits more than halved to $895m (£687m) in the third quarter and the firm said it would cut production of its 787 Dreamliner, blaming trade uncertainties.

Boeing boss Dennis Muilenburg was also stripped of his title as chairman by the board earlier this month, but remains as chief executive.

Source: BBC

Banner Content

Message from the CEO

On Internatonal Women’s Day

The mankind will not exist if there is no woman on this planet .Nature gave this power to woman to carry the source of existence.In today’s world even there are lots of awareness and activities to protect the rights of women there are still many evidence of discrimination and abuse for women . Women are still facing difficulties to live a decent and happy life . The physical or gender differences should not matter , what is most important is that we are all human being and Humanity is above all .

TV Channel

img advertisement

FOLLOW US

YOUTUBE

Advertisement

img advertisement

Social

Advertisement

img advertisement